Gfunk
Member
Ok, finally got the whole thing put together and hit the water today..
Here's a list of what we did.
-Removed the 1982 200hp blown Mariner and replaced it with a 2001 150hp Optimax. Both are 25" but the transom is a 20", seems to work ok, PO said he never had any problems, ran it this way for many, many years till it blew.
-Changed the water pump (man are there alot of bolts holding the Opti together)
-Installed the Humminbird 998 SI after a 3 hour odyssey removing the previous unit. The PO ran wires everywhere down both sides of the boat necessitating the removal of both rod lockers.
-Installed new Cabelas Big Man Seats (I left the low 300's awhile ago)
-Added (2) batteries in the cabin for the IPilot we added to the bow. Works great, had a 54" motor extended to a 60" and it works great. Had to cut the bow rail.
-Added homemade front bimini windshield, side curtains, and rear curtain.
-Added a removable trolling bar across the back.
After all that, I thought we had it pretty well together for a trip, so off to the lake we go for a sea trial.
Started off by backing the boat into the water and starting it, wanted to check my water pump impellar installation, so I walked back to check it out, it was working fine, but the water behind the boat was churning like the boat was in gear. Walked back up to take it out of gear and realized it already was. OOPS. An hour later, we had the lower unit off, the shifter connected and back in the water. On to the fishing!
Wrong. Picked my buddy up at the dock and realized that there was a fair amount of water in the splashwell and it was coming in through the scuppers into the boat. Bad. And to make it worse, the top of the transom cut out appeared to be just an inch or two above the water. Luckily we were close to the marina, so off we go. After a quick check of the bilge and some 1" drain plugs stuck into the deck drains to prevent the water from coming in, we were finally on the way to fish. Wrong again.
On our way from the marina, the alarm goes of on the Optimax. We were in a no wake zone, so I dropped the throttle a bit and it quit. Got into the wake zone, and hit the throttle and the alarm goes off again and it won't throttle up, I dropped it back to idle, throttled it up again and never heard the alarm again, a quick check of the water stream assured me that we were not heating up. Thought it was because we were idling, but later in the day we trolled with the main engine for about 2 hours without incident, so I'm assuming the impellar had to seat itself in or something. No idea.
I took some pics of the water in the splashwell to get some opinions on if this is normal or not. The pics don't do the problem justice, with me and my buddy back there the transom cap is only about 1" above the water. The current setup has 2 batteries in the hold right in front of the outboard, 1/2 a tank of fuel, my 300# buddy, me at 350#, and my 110# son. I think at the very least, I need to change the scuppers, but that won't fix the "butt heaviness" of the boat. As you can see in the pics, the drain holes in the transom are below the water line, and we occassionally got water over the transom.
Forgot to add, when we got it back on the trailer and pulled the plug,the bilge appeared to be just as dry as it was when we put it in.
Thanks in advance guys.
Here's a list of what we did.
-Removed the 1982 200hp blown Mariner and replaced it with a 2001 150hp Optimax. Both are 25" but the transom is a 20", seems to work ok, PO said he never had any problems, ran it this way for many, many years till it blew.
-Changed the water pump (man are there alot of bolts holding the Opti together)
-Installed the Humminbird 998 SI after a 3 hour odyssey removing the previous unit. The PO ran wires everywhere down both sides of the boat necessitating the removal of both rod lockers.
-Installed new Cabelas Big Man Seats (I left the low 300's awhile ago)
-Added (2) batteries in the cabin for the IPilot we added to the bow. Works great, had a 54" motor extended to a 60" and it works great. Had to cut the bow rail.
-Added homemade front bimini windshield, side curtains, and rear curtain.
-Added a removable trolling bar across the back.
After all that, I thought we had it pretty well together for a trip, so off to the lake we go for a sea trial.
Started off by backing the boat into the water and starting it, wanted to check my water pump impellar installation, so I walked back to check it out, it was working fine, but the water behind the boat was churning like the boat was in gear. Walked back up to take it out of gear and realized it already was. OOPS. An hour later, we had the lower unit off, the shifter connected and back in the water. On to the fishing!
Wrong. Picked my buddy up at the dock and realized that there was a fair amount of water in the splashwell and it was coming in through the scuppers into the boat. Bad. And to make it worse, the top of the transom cut out appeared to be just an inch or two above the water. Luckily we were close to the marina, so off we go. After a quick check of the bilge and some 1" drain plugs stuck into the deck drains to prevent the water from coming in, we were finally on the way to fish. Wrong again.
On our way from the marina, the alarm goes of on the Optimax. We were in a no wake zone, so I dropped the throttle a bit and it quit. Got into the wake zone, and hit the throttle and the alarm goes off again and it won't throttle up, I dropped it back to idle, throttled it up again and never heard the alarm again, a quick check of the water stream assured me that we were not heating up. Thought it was because we were idling, but later in the day we trolled with the main engine for about 2 hours without incident, so I'm assuming the impellar had to seat itself in or something. No idea.
I took some pics of the water in the splashwell to get some opinions on if this is normal or not. The pics don't do the problem justice, with me and my buddy back there the transom cap is only about 1" above the water. The current setup has 2 batteries in the hold right in front of the outboard, 1/2 a tank of fuel, my 300# buddy, me at 350#, and my 110# son. I think at the very least, I need to change the scuppers, but that won't fix the "butt heaviness" of the boat. As you can see in the pics, the drain holes in the transom are below the water line, and we occassionally got water over the transom.
Forgot to add, when we got it back on the trailer and pulled the plug,the bilge appeared to be just as dry as it was when we put it in.
Thanks in advance guys.